CHAPTER 16 AIRCRAFT REACTOR EXPERIMENT* The feasibility of the operation of a molten-salt-fueled reactor at a truly high temperature was demonstrated in 1954 in experiments with a reactor constructed at ORNL. The temperature of the fuel exiting from the core of this reactor was about 1500°F, and the temperature of the fuel at the inlet to the core was about 1200°F. The reactor was constructed before the mechanism and control of corrosion by molten salts had been fully explored, and therefore the experimental operation of the reactor was of short duration. Since the work was supported by the Aircraft Reactors Branch of the Atomie Energy Commission, the reactor was called the Air- craft Reactor Experiment (ARE).T The ARE was a thermal reactor in which moderation was accomplished by BeO blocks through which the fluoride fuel was circulated in Inconel tubes arranged in a symmetrical, heterogeneous matrix. The Inconel ves- sel containing the core was essentially a right cylinder, approximately 52 in. OD and 44 in. in height, with 2-n.-thick walls. The fuel passages consisted of l-in.-diameter Inconel tubes arranged in six parallel circuits, and each circuit, by the use of reverse bends at top and bottom of the core, made cleven passes through the core. The fuel passages did not traverse the peripheral BeO blocks which served as a reflector around the core of the reactor. A top view of the BeO blocks and the Inconel tubes is shown in Fig. 16-1. The moderator and reflector blocks were cooled by circulating liquid sodium from the bottom to the top of the pressure vessel. The sodium permeated all interstices of the BeO and flowed rap- idly through 1/2-in. vertical holes in the reflector sections of the BeO. An elevation drawing of the reactor which illustrates these features is presented in Fig. 16-2, and a photograph of the reactor vessel that was taken before assembly of the thermal shield is shown in Fig. 16-3. Since the purpose of the operation of this experimental reactor was to study the behavior of the circulating-fluoride-fuel system and to identify the problems associated therewith, the power output of the reactor was not utilized but, rather, was simply dumped as heat. The heat-removal svstem 1s shown schematically in Fig. 16-4. The fuel was circulated through a finned-tube radiator type of heat exchanger. This radiator was located within a sheet-metal housing of a toroidal shape. In another part of the toroidal housing there was a second finned-tube radiator through *By E. 8. Bettis and W. K. Ergen. 1R. C. Briant et al., Nuclear Science and Engineering, Vol. 2, No. 6, 795-853 (1957). 673 674 AIRCRAFT REACTOR EXPERIMENT [cHAP. 16 F1e. 16-1. Top view of the reactor core of the ARE. Hexagonal beryllium oxide blocks serve as the moderator. Inconel tubes pass through the moderator blocks to carry the molten-salt fuel. which plant water flowed. A large centrifugal blower circulated the coolant gas (helium) in the toroidal loop so that heat was picked up from the fuel radiator and dumped into the water radiator. An identical arrangement of radiators and blower was used for cooling the sodium used as the moderator-reflector coolant. In the interest of safety (for removal of afterheat in the event of a pump failure), the so- dium circuit was installed in duplicate so that an entire sodium cooling system was available as a spare. These two sodium loops were operated alternately during the experiment in an effort to keep a check on the op- erability of each loop. Had one loop failed to operate, the experiment would have been terminated for lack of a spare cooling system. The control system of the reactor was based on conventional practice. The three safety shim rods were actuated by electrically driven lead screws which moved electromagnets in a vertical plane. When these magnets were driven to their lowest extremity, an armature was engaged to which the shim (poison) rods were attached. Loss of current in the electromagnets would allow the rods to fall under the action of gravity into thimbles in the central region of the core. The regulating rod was a simple stainless- steel pipe which was rigidly attached to a rack driven by a reversible elec- CHAP. 16] AIRCRAFT REACTOR EXPERIMENT 675 Regulating Rod Assembly Safety Rod Assembly Fuel Inlet Manifold Reflector Coolant Tubes E 3 ’ j BeO Moderator nd Reflector Fuel Tubes | Thermal Shield E?A/Assembly Sooees . Fuel Qutlet Manifold 04 81216 et Scale in Inches Fig. 16-2. Elevative section of the Aircraft Reactor Experiment. tric motor through a pinion. Fission chambers located in the reflector, as well as ionization chambers located outside the pressure shell of the reactor, furnished the neutron and gamma-ray signals for the control system. The shim and control rods which entered the hot reactor core had to be cooled to prevent overheating from neutron capture and gamma-ray ab- sorption. This cooling was effected by circulating helium in a closed loop that included a water-cooled radiator, as in the case of the fuel and sodium circuits. This helium circuit was integral with a helium-filled monitoring annulus which surrounded all fuel and sodium piping in the system. This annulus was formed by putting a continuous stainless-steel sleeve around all hot piping, and the helium circulated in the annulus performed two functions: (1) it kept the hot lines at essentially an even temperature dur- ing the warmup period when the system was heated by means of electrical heating units placed on the outer surface of the annulus, and (2) the helium was monitored to ensure that the fuel and sodium piping was leaktight. Large, heated reservoir tanks were connccted to the system through isolation valves so that the sodium and the fused fluoride mixture could 676 AIRCRAFT REACTOR EXPERIMENT fcaap. 16 Fra. 16-3. View of the ARE Vessel before addition of the thermal shield. The external strip heaters with their electrical leads are shown in place. CHAP. 16] AIRCRAFT REACTOR EXPERIMENT 677 - Rod TN Actuator . i . Helium Pump | Helium Blower \ i Blower ; e . : | / - i ": Y i {7 . — T ao oo | Absorber Rod | ! L ~ n | ' c - T o 2 - oL e : @ | S 5 |=/|c o | 3 ] = | . o o o ’ o Water 5 5 X X Water ] 5 5 - ‘g F—— I T T T ; ) Reflector ‘ - . _Helium Reflector — Reflecter Coolant Fig. 16-4. Schematic diagram of the heat-removal system for the ARE. be pressurized from the tanks into the system and could be drained back into the tanks after the experiment was over. Dry helium was used for operating penumatic instruments and for pressurizing the liquids into the system from the tanks. Pumps for both the sodium and the molten-fluoride mixture consisted of sump-type centrifugal pumps with overhanging shafts. The pumps were mounted vertically, and a gas space was provided between the liquid level and the upper bearings of the pump. The pumps were located so that the free-liquid surface in the sump tank was the high point in both the fuel and the sodium eircuits. The sump tank of the pump also served as an expansion tank for the liquid. The isometric drawing of the fuel system presented in Fig. 16-5 indicates the relative levels of the components. Both of the liquid systems, fuel and sodium, were fabricated entirely of Inconel, and all closures were made by inert-gas-shielded electric-arc (Heliare) welding. The welding procedure was adopted after extensive experimental research and developmental work, and meticulous care was exercised in all welding operations. The entire reactor system, that is, the reactor vessel, heat exchangers, pumps, dump tanks, piping, and auxiliary equipment (with the exception of control rod drives), was located in con- crete pits below ground level. After the reactor was brought to criticality by manual fuel injection, concrete blocks were placed on top of the pits to complete the shielding of the system as required during power operation. Fuel was added as a molten mixture of Nal” and UF4 (enriched in U2%) after the sodium system had been heated and filled with sodium and the fuel system had been heated and filled with fuel carrier—a molten mixture of Nal’ and ZrFs. The fuel additions were made into the sump of the fuel pump through the use of a temporary enrichment system that was capable of injecting (by manual operation) a few hundred grams of fuel mixture 678 AIRCRAFT REACTOR EXPERIMENT [cHAP. 16 Standby Fuel Pump £E1Ed | S "~ Main Fuel Pump ¢ Frangible :{;"’-‘q. 7 g ) Disk Valve R T dog O — >, / 4 Heat > s 0 ‘k(\ Exchanger W o Frangible No. 2 o o Disk ngve/ B - : i / Heat EXChCIflQEr Ne. 1 p // . A % 57 T, - W, P Yr / LT > o Y S - ) /'\\ - Paie «}\ - 2 Vent / . o e el T oy Lol 7 Uy " Inlet—= ] ]/ &:xy”‘a/ o ~ ot = AU o el Carrier ) of fue Fill Line o Dump Tank I\ Reserve Tank No. 1 e Fill Tank No. 2 Fia. 16-5. Layout of the fuel system components for the ARE. at a time. This method of fuel addition was laborious and time-consuming, but it effectively and safely enriched the reactor to a critical concentration. The reactor was taken to criticality essentially without incident. The total amount of U235 added to the system to make the reactor critical was approximately 61 kg, but small amounts of fuel were withdrawn from the system for sampling and in trimming the pump level. The uranium con- centration at criticality was 384 g/liter of fluoride mixture. The calculated volume of the core was 38.8 liters at 1300°F, and thus the clean critical mass of the reactor was 14.9 kg of U235, It was demonstrated that the reactor had an over-all temperature co- efficient of reactivity of —6 X 1075 (Ak/k)/°F. As was anticipated, the fast negative temperature coefficient of reactivity (associated with the fuel expansion coefficient) served to stabilize the reactor power level. From a power lever of 200 kw upward, the temperature coefficient controlled the system so precisely that the reactor responded to load demands in a thoroughly reliable manner. The response of the reactor was demonstrated in a number of experi- ments, one of which is described in 1Mig. 16-6. The abscissa, to be read from right to left, is the time in minutes, and the print-outs from recorders giving the reactor inlet and outlet temperatures are the ordinate. Initially, in this experiment, the reactor was operating at low power. Then the heat CHAP, 16] AIRCRAFT REACTOR EXPERIMENT 679 Reactor Inlet and Qutlet Tube Temperatures hundreds of degrees F 0045 ™ T RS TN i T T T s b L [ [k R fl]i | 0040 F T T 1T T T 4 T IR Lobiefore b i et --.-«Shlm Rods Inserfed\ i 0035h hif | .| || | r*Fuel and Na BlowersOff‘ - T il et i Low Temperature i 3 0030 F | |ilfebnh oM i jlnierlockAutomuhcall i & TLT f‘*”*fjfi'k'“‘ e :‘ :‘ # - peduced Blower Speeg: ™~ 0025k Reactor LI vl Pq"l- Turned on Fuel System||! & lCooed s LT Helium Blower i 5 0020 k' Brought I+~ i r"t( ull Speec) zo 0015 HiCritical ‘" "‘, el Ll Lnser;red;ebgultfuhn? Rod; wa T T il| Reactor Subcritica [ :E):f:’:c‘:,ieo:;i—}: 1Ll ; ::g EEETurned Off Fuel Helium Jj 0010 o LT e T 7 *‘ngodm AR L L] e ol E:Iower | odium i g ST T T 0005 *"System [t {l I 3‘ . N *Jj'-i Moved Regu Iqhng Rod | Ty e LT T e Il 2400Jmmi- Ll T L R ;1}_: el . “H‘a'if !MIHSHII Hl > 2355k @; L e Ll Turned on Fuel System | a i ' ST M +"; H[1]i 4 Helium Blower | - 2350 Hj‘vi ot i ot i (Full Speed) g a5 i "{‘*l ; L | .i FH‘; Inserted Shim Rods = L ’l aiE | I ~ |Reduced Fuel System || 2340 [f a TR I "T|Helium Blower Speed i 3 AL ‘r ;."","E%IH l 1'-1.1,‘ to Zero 233510 4|0 e | ] Mli | 3 T T $5 [T & 2330111 | SLb e [3REsll hOperation at 2. * 395 Tube Inle! Tube Outlet} :.;f s l'lHt il g #Temperufure‘r Temperatvre@rp " | ii': T U G em e B T e o o i L Z Ll TN ‘!:VXLIU it Lt 2320T i “!\ \ T #‘a -+ lard Sodium System Hellum 9315 [T e - g {Blower on i S0 %'_J_'j« i LL‘ g | PSlowly Increase Fuel || 2310 L TP e T T Tk System Helium Blower e J ¥ L .4 Speed to Maximum 23051 L |1 B | Sl ‘ 1 o Reactor Critical: T 23007 Lt 3 | 1. JOperating at~200kw|...: T ‘ Tl : oy 2255 f——p R H : .!H ‘ Fic. 16-6. Chart of inlet and outlet temperatures for the ARE as influenced by various experimental procedures. extraction from the fuel was slowly increased and there was, first, a re- sultant decrease in the temperature of the fuel which reached the reactor inlet from the heat exchanger. This increased the reactivity and the re- actor power, as indicated by the temperature rise at the reactor outlet. The spread of inlet and outlet temperatures corresponds to a power level of 2.5 Mw. When the heat extraction was reduced, the inlet temperature 080 AIRCRAFT REACTOR EXPERIMENT [cHaP. 16 rosc and the outlet temperature fell until the two temperatures became nearly coincident. As may be seen, the control rods did not determine the power output; they only mfluenced the average temperature. Insertion of the shim rods decreased the temperature. Another rapid increase in the power demand on the fuel system again spread apart the inlet and outlet temperature recordings, and full insertion and full withdrawal of the regulating rod depressed and then raised both temperatures simultaneously. Next, the power extraction was stopped and the regulating rod wus in- serted to make the reactor suberitical. The third spread of the temperatures in I'ig. 16-6 was a result of a demonstration which showed that the reactor could be brought to eriticality, without use of the rods, by the power demand alone. Power extraction from the sodium system cooled the reactor to make it eritical, and power extraction from the fuel again caused the spread of inlet and outlet tem- peratures. The remarkable stability of the system made it unexpectedly possible to demonstrate that no more than 59, of the Xel'39 was retained in the molten fuel. It had been computed that the xenon poisoning after 27 hr of operation at full power would amount to 2 X 1072 in AL/k if all the xenon formed stayed in the fuel until it decayed. This level of poisoning was less than would be expected from the usual equations, partly because the fuel spent only one-fourth of the time in the core and was thus effec- tively only subjected to one-fourth of the flux, and partly because many of the neutrons had energies above the large Xe!'3 absorption resonance. As little as 59 of this computed poisoning would have been detectable, but none was found. There was a small leakage from the gas volume above the liquid surface of the fuel pumps which made operation at a high power level somewhat awkward, but danger to operating personnel was circumvented by operat- ing with the reactor pit at a subatmospheric pressure and remotely ex- hausting the pit gases to the atmosphere at a location where they were adequately dispersed. The entire program of experiments that had been planned for the reactor was completed satisfactorily. The reactor was shut down after a total power production of 96 Mwh, and it was later dismantled. The fuel and sodium systems had been in operation for a total of 462 and 635 hr, re- spectively, ineluding 221 hr of nuclear operation, with the final 74 hr of operation in the megawatt range.